fanuc 400 error code Hilda South Carolina

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fanuc 400 error code Hilda, South Carolina

was executed)095No P type can be specified for program restart (because after program interruption, external work zero point offset value changed)096No P type can be specified for program restart (because after Reply With Quote 12-21-2012,05:03 PM #5 Smileyvit View Profile View Forum Posts Registered Join Date Aug 2008 Posts 4 We have the overload problem fixed. Any advice would be great and please assume nothing as I do not know my way around the machine yet! Still no good.

Al. also note, if 5 wires on CN1, then the 'toh' jumper on the drive should be open. Some additional info: I was asked to check diagnostic 802, which read a non-zero value (diag 800 and 801, which are X and Y drive diags respectively, both read 0 or First one was yesterday when the machine had a part finished and was waiting for me to load another one.

The 400 alarm is for servo overload-doesn't seem to be the case here, axes are all lubed, taking light cuts, and no trips of the breakers. tach is either bottom or right of the three pots. What I am not sure is how to test the cable, drive connector. Reply With Quote Quick Navigation Fanuc Top Site Areas Settings Private Messages Subscriptions Who's Online Search Forums Forums Home Forums Policies / FAQ CNCzone's Community Policies FAQ Events, Product

The time now is 02:53 PM. Register Forgot password? Or the velocity command value of the DA converter is out of the range of +8191~ - 8192. Perform manual reference point return again410The content of error register of the X axis is larger than the value allowed while the machine is stopped411The content of error register of the

Generated Fri, 14 Oct 2016 01:40:06 GMT by s_ac5 (squid/3.5.20) Or the velocity command value of the DA converter is out of the range of +8191~ - 8192. You may have to register before you can post: click the register link above to proceed. Reply With Quote 05-18-2013,11:09 PM #5 Render View Profile View Forum Posts Aluminum Join Date May 2012 Location New Zealand Posts 60 Post Thanks / Like Likes (Given) 9 Likes (Received)

Incorrect settings will cause this alarm444The resolver/inductosyn position detecting system of the 4TH axis is trouble425A feed rate exceeding 511875 detection units/sec was commanded in the 4TH axisAn incorrect setting of SHOW EASTEC Fabtech Cabin Fever DEADBEAT ADVERTISERS Ebay Ads Here Polls Environmental / Alternate Energy Videos Web Deals/coupons Want To Buy...Need help! Got a 400 servo alarm on a Fanuc 6M. Portals IndustryArena Sheet Metal Working Grinding Software Tools Technology Automation Composite Additive Manufacturing Forum Categories All Forums Webinars Supplier Supplier Overview Premium Newsrooms Become company member Marketplace Used machines Sourcing Jobmarket

thats my 2 cents for the night Last edited by tc429; 10-27-2011 at 10:06 PM. Does it take longer for it to trip if its turned past? This particular problem is a major machine problem but was utterly simple to fix, and despite warnings from the forum about failing and defective drives or servos, it was nothing of note, gain pot 99% of the time should run near straight up- if you start seeing it turned by more than a click either way, something might be screwed up. [*note-

I checked all the breakers/thermal resets. members Home IndustryArena - Network for Manufacturing Industry Themes Tools Technology Sheet Metal Working Grinding Software Automation Additive Manufacturing Composite Industry 4.0 Home Forum CATEGORY OVERVIEW FORUM LIST 100 latest forum Another case change connection unit)602PC program has not yet been loaded603The correspondence between NC and PC is incorrect or interrupted. The one axis that was tripped has a 20M motor on it.

After a bit of playing around turning the control off/on a few times the alarm was gone. Practical Machinist is the easiest way to learn new techniques, get answers quickly and discuss common challenges with your peers. Happened again a few hours later, pulled the covers off and all the paint on the motor housing had peeled off due to the heat and you could have fried an Fixed the problem by replacing the axis motor haven't had an issue since.

CNC, Mechatronics Integration and Custom Machine Design “Logic will get you from A to B. Any suggestions would greatly be appreciated. Where do I put the other lead of my meter on, to any ground? Imagination will take you everywhere.” Albert E.

The site is 100% free to join and use, so join today! This alarm happens if yout drive modules become weak which drive you are using and what is the alarm on drive harsh Reply With Quote 11-23-2006,02:32 PM #5 darrylh View Profile Ask others by posting in the CNC Professional Forum CNC Control OEM's GE Fanuc Mitsubishi Yaskawa Home Fanuc Yasnac / Yaskawa Mitsubishi CNC Training Books Search (sites) Copyright © 2008-2016 CNC Thread Tools Show Printable Version Subscribe to this Thread… Search Thread Advanced Search Display Linear Mode Switch to Hybrid Mode Switch to Threaded Mode 05-17-2013,08:41 AM #1 Machinery_E View Profile

I believe I am looking for 24volts on the OVL contacts if the drive is okay...not sure which pins...I think its 3? ideally values will be flickering 0 +/-1, if so, go to next axis (if any servo is 'buzzy' might need to decrease gain on that one, then match others to it. note value again. Imagination will take you everywhere.” Albert E.

Probably about 6 hours later, right in the middle of a cut the same alarm came up. The Fanuc engineer informed me that alarm 400 was the Z drive (not X, as I was advised on this forum). Engines Musical Instrument Design and Construction Jet Engines and Ram Jets Parts for Radio Control Models RC Robotics and Autonomous Robots Steam Engines Stirling Engines International Forum Brazilian CNCzone Spanish CNCzone But again, does not make sense since there are no tripped breakers or alarms on the amps.

The 'pots' on the Z drive board were labelled R1, R2, and R3, which were all set to about 2 O'clock. if the rpm is the same on a solid dc source, the motor will build the same torque in both directions. In that time the x axis motor had cooled enough to run the machine. Become a forum member.

On both drive boards, there are a small number of potentiometers or 'pots', which increase the 'gain' on the drive. Push the reset button after turning off the switch.101The power was turned off while rewriting the contents of memory in the part program storage & editing operation. any steady values in 800-802 are a sticky slide most of the time, will cook a motor...increasing gain will help it pull into position, but I'd be sure the slides are Please try the request again.

Attached Thumbnails CNC, Mechatronics Integration and Custom Machine Design “Logic will get you from A to B. I have an identical machine, so I took the cable off of it, and still the same problem. I was told to change R1 and R2 to about 12 O'clock and switch on. Now we are having a problem with the Z-Axis not wanting to reference to home without holding down the Z plus button.

All looked good.